Today was a Saturday and so I got a lot done on the
                  '53 25 hp Evnirude.
                
                  
                     
                        click to enlarge 
                        images | 
                  
                
                After a 2 hour morning "paddle" aboard the Larsboat 
                  on a local river, I comenced to working on the 25; first order 
                  of business was to remove the carburetor for cleaning and rebuilding. 
                  The carb on this 50-year-old engine is about as simple as these 
                  things get; removing it required the disconnecting of the linkage 
                  that synchronizes the carb butterfly valve and the magneto "spark 
                  advance" and the removal of just two nuts. I always suggest 
                  disconnecting linkages in such a manner so as not to disturb 
                  adjustment settings, and so I merely removed a tiny cotter pin 
                  on a bellcrank and unhooked a little tie rod.
                  
                  
After 
                  removing the two nuts and also the fuel feed hose, the carb 
                  was removed from the engine and dissasembled. All in all, it 
                  did not look too dirty, but I went ahead and dropped it into 
                  a gallon container of carb. cleaner to let it soak while I worked 
                  on other things.
                  
                  
Usually 
                  I just spray-out carbs with an aerisol carb cleaner, which is 
                  the way that most engine manufacturers recommend cleaning late-model 
                  carbs; in the old days, one allowed a carb to soak in cleaner 
                  and then blew-it out with compressed air. A carb allowed to 
                  soak for a day or two in the "old" carb cleaners came 
                  out looking like brand-new, but it is difficult to find the 
                  "old" cleaners now, as they have been replaced by 
                  'environmentally-friendly" carb cleaners that do not clean 
                  as well.
                  
                  
While 
                  waiting for the carb to soak, I decided to replace the water 
                  pump impeller. The six bolts that mount the lower unit were 
                  removed, and the lower unit allowed to drop down to the extent 
                  that the shift rod would allow. The shift rod is what connects 
                  the shift lever on the Starboard side of the motor to the lower 
                  unit, which is where the actual "transmission" is 
                  located.
                  
                  
This 
                  is where later OMC engines have an slight advantage; they usually 
                  have a small access door in the side of the "tower" 
                  or exhaust housing which allows one easy access to the coupler 
                  that needs to be disconnected in order to remove the lower unit. 
                  The Big Twin does not have such an access door. The coupler 
                  is disconnected by allowing the lower unit to drop as far as 
                  it can, and then by reaching into the open void between the 
                  tower
 
                  and lower unit with a screwdriver and disconnecting the coupler. 
                  Really no big deal when removing the lower unit, but a farely 
                  major problem when re-installing it.
                  
                  It is bad practice to carry a lower unit by holding the driveshaft; 
                  in the case of this particular engine it, the driveshaft is 
                  not secured into the lower unit by anything other than the tiny 
                  key that drives the impeller.
                  
                  
With 
                  the lower unit off the engine, the four screws securing the 
                  pump housing were removed, and the pump housing and impeller 
                  slid-up off the driveshaft. Most of these old OMC's have an 
                  "O" ring sitting in a groove milled into the splines 
                  at the 
top 
                  of the driveshaft. the purpose of this "O" ring is 
                  to prevent water from rising up the driveshaft and getting into 
                  the crankshaft bearings in the powerhead. The "O" 
                  ring needs to be removed in order to remove and reinstall the 
                  pump housing and impeller, but be sure to replace it once you 
                  are finished with your waterpump work. 
                  
                  
The 
                  impeller removed from the engine was obviously "toast" 
                  with the blades retaining a curled shape, and one blade retaining 
                  a backwards-curled shape. Obviously, this impeller had seen 
                  better days. With new impellers readily available from both 
                  Johnson and Evinrude dealers, and also through aftermarket suppliers, 
                  it just does
 
                  not make any sense to chance using an old impeller, even one 
                  that looks in better shape than this one did. I installed a 
                  new Sierra-brand impeller and reinstalled the pump housing and 
                  also the "O" ring on top of the driveshaft. A SMALL 
                  dab of waterproof grease was rubbed onto the driveshaft splines; 
                  don't over-do it.
                  
                  Getting the lower unit back onto the engine took a bit of "engineering." 
                  One has to hold the lower unit just below the level of it's 
                  installed position while one inserts the screw into the shift 
                  rod coupler and tightens it, while also halding a flashlight 
                  so as to see inside the engine. I hunted up a bolt of the same 
                  diameter and thread as the lower unit's mounting bolts, but 
                  which was longer, and used this long bolt to hold the lower 
                  unit onto the engine but allowing about a 3/4 inch gap between 
                  the mating surfaces which then allowed me to focus a flashlight 
                  on the couple while I inserted the screw using a magnetic screwdriver. 
                
                
                Once the coupler was fastened, I secured the lower unit into 
                  place with it's proper mounting bolts and removed the one long 
                  bolt. Although dealing with the coupler is easier on MOST later 
                  OMC's, one advantage of this older engine is that it did not 
                  utilize a water tube for conducting water from the pump up into 
                  the powerhead, and dealing with the water tube can sometimes 
                  be difficult on the later engnes. Onc must simply take one's 
                  time and not allow frustration to take-over when reinstalling 
                  lower units.
                  
                  
At 
                  this point I went back to the carb, which had been soaking for 
                  about an hour or so. The passages in the carb were blown-out 
                  with aerisol carb cleaner (BE SURE TO WEAR EYE PROTECTION !!!) 
                  and I went looking for a carb kit. The Sierra catalog does not 
                  list a carb kit for a '53 Big Twin, but does list a kit for 
                  '54s. I used a "54 kit which had many extra parts not needed 
                  for the '53, and I needed to trim the bowl gasket a bit with 
                  a razor blade in order to make it fit, but I did replace the 
                  parts that needed replacing; 
primarily 
                  the bowl needle and seat, the afore-mentioned bowl gasket, and 
                  the packing that seals the high - and low speed needle valves. 
                  The existing float looked OK, as most do; keep in mind that 
                  these old cork carb floats are coated with varnish, and that 
                  carb cleaner is intended to remove varnish, so keep the cleaner 
                  away from the float..
                  
                  
The 
                  reassembled carb was bolted back onto the engine and the linkage 
                  reconnected. On these old OMC engines, the twist-grip throttle 
                  is connected to the magneto, and advancing the twist grip advances 
                  the magneto timing. The linkage connecting the carb butterfly 
                  (throttle) valve needs to be synchronized to the magneto in 
                  order to obtain the best performance. On this engine, as on 
                  so many old OMc's, that is a simple matter of lining-up a mark 
                  on a sheet-metal "cam" screwed to the underside of 
                  the magneto, with the roller or follower on the linkage for 
                  the butterfly valve. One retaining hole in the sheet metal cam 
                  is slotted so that the cam may be moved in and out, and the 
                  cam is moved so that, when the butterfly roller is next to the 
                  mark, any slack or "looseness" in the linkage to the 
                  butterfly has been "taken up" and the butterfly shaft 
                  itself just begins to move. Making this adjustment takes all 
                  of 5 minutes and requires no tools other than a small wrench 
                  to fit the cam's retaining screws.
                  
                  Now it was time to finally reinstall the 
                  magneto, a procedure made considerably more complicated by this 
                  early engine's tension-cable linkage to the twist grip. As previously 
                  mentioned, later engines use a shaft and bellcrank arrangement 
                  which is much easier to deal with. Other than getting the cable 
                  back onto it's sheaves, mounting the magneto involved no more 
                  than placing it down onto the crankshaft, being mindful of not 
                  allowing the "followers" on the new ignition points 
                  to "hang-up" on the cam which actuates them, and refastening 
                  the four screws which secure the magneto. The flywheel was set 
                  in place and lightly secured by it's nut, then the flywheel 
                  was slowly rotated by hand to insure that the coil "heels" 
                  did not make contact with the flywheel magnets (they did, and 
                  the flywheel was removed and the coils moved back away from 
                  the flywheel a merest thousand of an inch; see magnetos 
                  column for more details)
                  
                  
With 
                  the flywheel again set on the crankshaft and the nut hand-tight, 
                  "flipping:" the flywheel by hand produced sparks from 
                  both sparkplugs. A magneto that sparks this readily makes engine 
                  starting less of a chore.
                  
                  With about 3 1/2 hours expended on the engine today, the replacement 
                  of old fuel lines will wait until the next session, amd at that 
                  point the engine will be about ready for the initial starting 
                  attempts. Once the engine has (or has not) proven that it will 
                  run, I will then have a look at the recoil starter to see what, 
                  if anything, it needs.
                Max
                Continue 
                  on to Part 3....