I have been wanting to sit down and actually write 
                an article for Duckworks for some time. Today I was out running 
                my 54' 7.5 evinrude and 58' 18 Johnson seahorse for the first 
                time this year. I guess I got the bug to finally sit down and 
                write about the 18hp spark plug hole repair I did late last year. 
              Before I get to the details of the repair, I would like to give 
                a brief background on my 58' 18hp Johnson Seahorse. I received 
                this motor for free from my Grandfather. He had gotten it from 
                his cousin 15 years earlier, rescued from under an oak tree, where 
                it had been for an undetermined number of years. Needless to say 
                it hadn't been run in a very long time and was in rough shape. 
               
              
                 
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                  Rough Shape | 
                 
               
              When I got it home, I dropped this sad looking little motor into 
                the test barrel and began a couple of basic tests. It had both 
                compression and spark, so I connected my gravity fed fuel source 
                to the carb inlet and began pulling on the blister maker. After 
                10 or so pulls, nothing, not even a pop. I then carefully drizzled 
                some fuel directly into the intake, and vroooom away she went. 
                I tinkered with the fuel settings for a minute or so and had it 
                idling. I had to shut it down rather quickly due to the water 
                pump, or lack there of, but I at least now knew it was worth spending 
                a dollar or two to see if it could be pushed back into reliable 
                service.  
              I went to my local NAPA and purchased the water pump/impeller 
                and a couple of spark plugs. I referenced Max's 
                article here on Duckworks to install the impeller, 
                thank you Max and a tip of the hat. 
              
                 
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                  Socket Wrench - Easy Does it. | 
                 
               
              My trouble started when I went to disassemble everything to install 
                my parts. I found that the motor had been used in South Mississippi 
                in brackish/salt water and put away without any sort of cleaning. 
                I was able to get it apart with several broken bolts and few choice 
                French words along the way. I had to make some "modifications" 
                to get it back together. NO, they aren't pretty and NO, I wouldn't 
                recommend anyone use them.  
               Now that the impeller housing problem seemed to be resolved, 
                I went to install the new plugs. This is when I discovered that 
                the bottom spark plug hole was stripped out and only had about 
                1 1/2 threads actually holding the plug in the head. The new plug 
                wouldn't hold in the head, as it is just a little bit shorter 
                than the older plug that came in it. Well I really wanted to see 
                if my "modifications" were going to work and hold up 
                so I put the old plug back in the bottom hole and ever so carefully 
                snugged it up. I completed my test run for the impeller, which 
                worked out just fine. 
              
              Later that night I began to do a little research for spark plug 
                hole repair on outboard motors and there isn't much info out there 
                for outboards. Knowing that the plug hole was a standard size, 
                I refined my research to plug size and found several kits. I settled 
                on the Helicoil Save-a-thread. It cost me about $20 plus shipping. 
              
              This is a very simple and easy tool to use. I was able to make 
                the repair without removing the head. I know that If I ever have 
                to pull the head on this motor it will probably be relegated to 
                the parts motor status due to the salt water exposure I mentioned 
                earlier.  
              
              Now on with the repair.  
              First, lets start with a little safety. Safety glassed are always 
                a must and gloves would be a good idea also. Clamp your motor 
                to a stable work station. A saw horse will do nicely and you could 
                even leave it clamped to the boat, but would be easier on a saw 
                horse. Remove the motor cover. Remove the plug. Carefully turn 
                the flywheel so that the piston for the cylinder you are working 
                on is at the bottom of it's stroke. Now take the tap/threading 
                tool and find your 3/8 ratchet to drive the tool. Now apply a 
                light coat of grease to the recessed grooves, this is to help 
                catch the aluminum shavings you are about to create.  
              Start the tool carefully and straight in the plug hole by hand, 
                now use the ratchet to slowly begin to cut the threads for the 
                insert. Once the tool has cut the hole, remove the tool and inspect 
                for small shavings that may have fallen into the cylinder or shards 
                at the bottom of the hole that may break off later while running. 
                Shavings can generally be removed with a little compressed air 
                and shards with needle nose pliers.  
              You are now ready to install the insert. Apply a small amount 
                of RTV silicone of you choice to the threads of the insert. It 
                just needs to be of the high temperature variety. Thread the insert 
                all the way into the newly cut hole. Take the supplied driving 
                tool and stick it into the insert and carefully hit it with a 
                hammer. You are only trying to spread the thin mild steel knurled 
                portion of the insert, so you don't need to get the biggest hammer 
                you own. Cracking the head would surely ruin your day so don't 
                get carried away. Wipe away any silicone that squeezed out. Let 
                the motor sit overnight to allow the silicone to cure.  
              Now all that is left is to reassemble the motor and give it a 
                test run. I think it took me about 20min to make the repair, and 
                this included actually reading the instructions that came with 
                the tool. I hope this saves someone some aggravation and keeps 
                another one of these great ole' motors humming.  
                
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