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                “Start to Finish”  
                Part IV 
               With the lower unit removed form the engine 
                and clamped in a well-padded vise, I removed the roll pin from 
                it’s hole near the top of the vertical driveshaft. This 
                pin is what the seal hardware on the top of the driveshaft sits 
                on. The pin needs to be removed in order to slide the pump body 
                and impeller up off the driveshaft. The pump body itself is held 
                down with 4 screws. Remove the pump body and old impeller and 
                be mindfull of the tiny key on the driveshaft which engages the 
                impeller.  
              If the pump body does not look too scored, it can be reused (I 
                almost always reuse the old pump body) There will also be a tiny 
                passage in the pump body that allows water from the puimp to flood 
                a cup surrounding the driveshaft. The water in this cup is what 
                seals the driveshaft to the pump body and you should make sure 
                that the tiny hole that supplies this water is not plugged.  
              Also check the metal plate under the impeller for wear - I have 
                occasionally replaced the plate. 
              Slide the new impeller down the shaft and then the pump body 
                down over it. Make sure the impeller has engaged it’s drive 
                key. The easiest way to get the pump body down over the extended 
                fins of the impeller, without causing the impeller to come off 
                the drive key, is to gently push down on the pump body while manually 
                turning the driveshaft in the direction of normal rotation (clockwise 
                when looking down on the shaft.) the fins will fold back and the 
                pump body will drop down until it is fully seated. Screw the pump 
                body down and put the pin back in the top of the driveshaft. 
              The tube that conducts water from the pump up to the powerhead 
                should have stayed installed up in the “leg” of the 
                motor when the lower unit was removed. If the tube came out attached 
                to the pump body, pull it loose from the pump and insert it up 
                in the “leg”. Make sure that the rubber grommet in 
                the pump body looks decent, or replace it. I reused the old one 
                on the Johnson. 
              As you install the lower unit back on the engine, you need to 
                make sure that the driveshaft and the shift shaft go up where 
                they are supposed to, and you must be sure that the water tube 
                is seated in the grommet on the pump body. With the Johnson, it 
                took me a few tries to get all of this done. Try to have the outboard 
                vertical when you do this, and a good light helps. 
              Once the lower unit was bolted back on the Johnson, I connected 
                the shift linkage up and placed the seal components back on the 
                driveshaft. then I reinstalled the powerhead, using a new gasket 
                underneath it. The gasket under the power head directs cooling 
                water to where it should be, and keeps it out of where it shouldn’t 
                be. The gasket also plays a large part in determining the amount 
                of crankshaft “end-play” (remember from part 
                2?) Too thin a gasket can reduce end play to the 
                point where there is extra wear on the crankshaft and bearings. 
              With the lower unit and powerhead back on, I was finally ready 
                to try to start the engine for the first time. The motor was clamped 
                to a drum of water, and after a few pulls and some needle valve 
                adjustments, it started up and idled well. 
              But there was not much water being sprayed from the exhaust bypass, 
                which is the cooling water indicator for this engine. After a 
                few minutes running, I tried touching various areas of the cylinder 
                head and block with a Thermomelt crayon which melts at exactly 
                175 degrees F. If the engine was running “cool,” the 
                crayon should not have melted, but it did. I had a over-heating 
                problem. 
              I removed the power head , and put the “headless” 
                outboard back into the water barrel. I chucked my cordless drill 
                to the protruding driveshaft and spun the shaft with the drill 
                to see if the pump would shoot water out the top of the water 
                tube. It barely trickled out. 
               I removed the lower unit and the pump body to make sure that 
                the impeller was engaging it’s drive key, but that did not 
                appear to be the problem. The pump body does not have any sort 
                of gasket to seal it, and thinking that the body may have warped, 
                I used some ‘gasket in a tube” to seal the pump body 
                down on it’s base. I also replaced the water tube grommet 
                in the pump body. 
              With the “headless” outboard back in the water barrel 
                and the cordless drill reattached to the driveshaft, I got a stronger 
                trickle of water but not near what it should have been. I put 
                the power head back on and started up the motor and the Thermomelt 
                crayon still indicated an overheating engine. 
              The water intake screen directly behind the propeller appeared 
                to be clear, so I removed the rectangular cover on the lower unit 
                that serves as a water intake when the motor is in reverse and 
                discovered crud almost completely blocking the water passages. 
              I cleaned the crud out with a screw driver, put the reverse intake 
                cover back on, started up the motor and it ran cool. the Thermomelt 
                crayon did not melt. 
              After about 30 minutes of ‘bucket cruising,” the 
                engine had proved itself worthy for ‘boat testing,” 
                but before I do that, I like to have a look at the recoil starter, 
                the part of an outboard that seems to take the most abuse, and 
                give the most trouble. 
              The starter rope was an old one; cotton fiber over a metal wire 
                core, so I decided to replace the rope and also the recoil starter 
                spring. Once removed, the old spring demonstrated it’s age 
                by retaining a coiled shape, and the rope was replaced with ordinary 
                nylon braided rope. This work was accomplished on a Saturday morning, 
                less than one week after the Sunday degreasing of the motor. 
               
                At some point in it’s life, the lower unit of this outboard 
                had been painted a copper color- I suspect to match the copper 
                bottom paint on a wooden boat. Of course, everyone knows that 
                one should never paint an aluminum outboard motor with a copper-based 
                anti-foulant paint because of the risk of corrosion, so I assume 
                that an ordinary enamel was used. 
              A couple years ago I bought several cans of automotive spray 
                paint at a Big Lots closeout store because the colors appeared 
                to be close to those of some old outboard motors, and anyway the 
                paint was only 29 cents a can. I used some General Motors green 
                paint, over zinc-chromate primer, to repaint the outboard from 
                the bottom of it’s cowling down. Then I clamped the motor 
                onto the auxiliary motor bracket on my AF4 in preparation for 
                the upcoming Midwest Messabout, which would be the motor’s 
                first test on a boat. 
              During the Messabout, the little Johnson was run for about 45 
                minutes total time, on two different days. It preformed well with 
                no problems arising, and will now serve as my auxiliary engine 
                for the AF4, replacing a 1958 Johnson 3 hp which was really too 
                small to push the boat against current and wind. 
               
                It has been said that there are no guarantees in life, and certainly 
                there are no guarantees that the old outboard that you buy will 
                turn out to run just as sweetly as this one has (in fact, this 
                one could “blow-up” next week), so if you want a guarantee, 
                you are going to have to buy a new outboard. But considering that 
                I paid 50 dollars for the motor, and put about 80 dollars or so 
                (retail) worth of parts into it, I don’t really have all 
                that much at risk. And those new parts could be transferred to 
                another old OMC engine, should the need arise. I have a couple 
                of early ‘50s Evinrude 15’s that both make an awful 
                bearing noise; At some point in the future, if I can not repair 
                the problem, I will pirate the new parts installed in them for 
                use in other engines. 
              Working on old outboards does not entail rocket science; these 
                engines are about as “low-tech” as tech can get 
              With a good manual and some studying and some thought, you can 
                do this. 
              Later 
              Max 
                
              Parts used to repair 1955 Johnson 5.5 
                hp outboard; 
              
                 
                  | Item | 
                  Sierra part number  | 
                  List price  | 
                 
                 
                  | Gasket  | 
                  18-2901  | 
                  $3.00  | 
                 
                 
                  | Impeller | 
                  18-3001  | 
                  $15.40  | 
                 
                 
                  | Tune-up kit | 
                  18-5006  | 
                  $18.00  | 
                 
                 
                  | Recoil spring | 
                  18-6501  | 
                  $8.60  | 
                 
                 
                  | Carb kit | 
                  18-7043  | 
                  $12.70  | 
                 
                 
                  | Fuel filter | 
                  18-7828  | 
                  $4.45  | 
                 
               
              (2) Champion J8C spark plugs 
                (3) ft copper-core spark plug wire 
                Misc. small hose clamps 
                Misc. fuel hose 
                Nylon rope (for starter) 
                Rubber bushing for pump housing 
                Gasket sealant. 
              NOTE The cracked magneto coils were replaced with 
                “Used but good” coils I had on hand. 
                New Sierra coils, part # 18-5181, list for $21.45 each 
                Often, “Used but good” coils can be purchased at 
                swap meets for much less, or a cheap” parts motor” 
                may supply you with coils (as mine did). 
              You should be able to find a boat dealer 
                willing 
                to sell the Sierra parts for slightly less than list price; 
                be sure to shop around. 
                
              
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